Category Archives: Testing

K04 Dyno Baseline

This morning the S4 went back onto the DynoJet dyno for a series of pulls with the BorgWarner K04’s and a moderate boost Daz tune.

The purpose of this session was to establish more baseline data for making comparisons to some aftermarket turbocharger options.

Chart of BW K04 baseline dyno pulls
BW K04 baseline dyno pulls

The ‘final’ results peak dyno numbers are of less interest to me than the shape of the torque curve.  I am expecting a K04-hybrid turbocharger to be capable of more peak torque and power than the RS4 K04.

Here is the boost profile that this tune uses:

Chart of K04 Stg3 tune boost profile
K04 Stg3 tune boost profile

 

Boost and MAF

Boost & MAF
Boost & MAF

 

Boost and N75 Duty Cycle

Boost & N75DC
Boost & N75DC
Note: The PID was calibrated for loads experienced on the street since tuning was not done on a dyno. The load presented by the Dynojet differed from that on the street. The boost / torque oscillations seen on the dyno are not replicated on the street.

Here’s a street pull:

street_54F

Here is how the K04’s compare with K03 turbochargers on my car.  K03’s are shown with two different tunes, one very aggressive and the other moderately aggressive.

K03 (NVR & Nef tunes) vs K04 (Daz tune) Wheel Torque
K03 (NVR & Nef tunes) vs K04 (Daz tune) Wheel Torque

What is notable about the chart above is how closely the torque curve of the K03 and K04 match one another.

K03 (NVR & Nef tunes) vs K04 (Daz tune) Wheel Horsepower
K03 (NVR & Nef tunes) vs K04 (Daz tune) Wheel Horsepower

 

Below are the EGT readings for each turbocharger/tune on the dyno.

Chart of K03 vs K04 EGT readings on dyno
K03 vs K04 EGT readings on dyno

Wheel well pressure

While in the process of removing the shroud from my test intercooler I realized it would not take much additional effort to relocate a couple of pressure sensors to the wheels wells to check a claim that there is a high pressure region in front of the tire that hurts air flow through the intercooler core.

Shown below are the locations that the sensors were placed in the wheel well liner slats.

picture of driver side wheel well
Driver side wheel well liner
Picture of passenger side wheel well liner
Passenger side wheel well liner

After placing the sensors in the wheel wells I set out on the same route I have driven previously for the IC shroud testing to collect IC MAF data.

Results:

Shown below is the pressure reading from each sensor during the drive.

Chart of Audi B5 S4 wheel well pressure

Effectively there was no positive pressure recorded by either sensor.  The values shown on the chart (red and blue lines) are within the sensors measurement error.  Possibly a more sensitive device, one that could accurately read less than 1/10 psi of pressure, could have shown a change with different speeds.

The one period where the passenger side pressure rose to approximately 0.05 psi may have coincided with the S4 passing another vehicle resulting in a momentary increase in pressure.

The other results that were obtained are related to the mass air flow through the intercooler core.  This case had the shroud removed from the intercooler and the belly pan in place.

Chart of intercooler shroud final data

Overall the results of this testing have produced some peculiar trends that suggest there are some not-so-obvious air flow interactions taking place through the bumper cover and below the vehicle.

 

IC Shroud Test – Cleaned Up Data

Following up on the initial results that were recorded to assess the mass air flow through a portion of the intercooler core.  The raw data included various speed changes and spanned several minutes worth of driving, both of which made comparing the different configuration results challenging.

Chart of shrouding maf test
Shrouding MAF Test

 

Presented below is data that has been sifted through to extract specific conditions so as to allow a direct comparison of like cases.

For each speed I found the median value for the time period that the speed was being held, and for the accompanying MAF readings I also found the median value.  These are presented on the chart as discrete points and then connected by lines to help with illustrating the trend.

It can bee seen that there is some variances in speed between the different conditions, i.e. one case may have a median speed of 39.8 mph while a comparison case has a median value of 40.4 mph.  Holding the exact same speed on the road at different times would be hard achieve and I believe the results are close enough to represent the underlying truth values.

Chart of intercooler shroud comparison data

The chart illustrates a couple of interesting points.

  1. That the addition of the shrouds improves the mass airflow through the section of the core that the MAF is located behind.
  2. Going from 30 to 40 mph for the case without shrouds shows a drop in mass air flow.  (Air flow into the area forward of the IC core or pressure behind the core is likely being disrupted by some interaction with another part of the vehicle.)
  3. Even at 50 mph the case without shrouds has not recovered to the air flow rate recorded at 30 mph.
  4. All test cases show a drop in air flow going from 55 to 60 mph.  (This is likely another secondary interaction that is impacting the air flowing through the core.)
  5. All three cases show roughly the same increase in air flow through the core versus speed increase.  If the 30-40 mph drop in the case of the “No Shrouds” had not occurred the rate of increase in mass air flow rate would have mirrored the other two cases closely.
  6. Above 30 mph the absence of the belly pan appears to have improved airflow through the IC core.

Conclusion:

These results show a clear benefit to having the shrouds installed for increasing mass air flow through the section of the intercooler core where the MAF sensor and housing were placed.

The results don’t give any indication as to the affect of mass air flow rate on intercooler performance, and subsequently the charge air intake temperature.  It is possible that a mass air flow rate of 5 g/s is adequate to transfer away the maximum amount of heat available across the core fins and that additional air flow in excess of that amount is unusable, therefore not decreasing the intake air temperature any further.